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Investigation finds Suncor’s Colorado refinery meets environmental permits


These translations are done via Google Translate

DENVER (Reuters) – A Colorado refinery owned by Canadian firm Suncor Energy Inc meets required environmental permits and is adequately funded, according to an investigation released on Monday into a series of emissions violations at the facility between 2017 and 2019.

The 98,000 barrel-per-day (bpd) refinery in the Denver suburb of Commerce City, Colorado, reached a $9-million settlement with the Colorado Department of Public Health and Environment (CDPHE) March 2020 to resolve air pollution violations that occurred since 2017. That settlement also addressed an incident in December 2019 that released refinery materials onto a nearby school.

As part of the settlement, Suncor was required to use a third party to conduct an independent investigation into the violations and spend up to $5 million to implement recommendations from the investigation.

Consulting firm Kearney’s investigation found the facility met environmental permit requirements, but also pinpointed areas for improvement, including personnel training and systems upgrades, some of which was already underway.

“We need to improve our performance and improve the trust people have in us,” Donald Austin, vice president of the Commerce City refinery said in an interview, adding that the refinery had already undertaken some of the recommendations from the investigation.

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In mid-April, Suncor will begin a turnaround at the facility that includes an upgrade to a gasoline-producing fluid catalytic cracking unit (FCCU) at Plant 1 of the facility. That turnaround is anticipated to be complete in June 2021.

Suncor last year completed a similar upgrade of an automatic shutdown system for the FCCU at the refinery’s Plant 2.

By 2023, the company will also install an additional control unit, upgraded instrumentation, automated shutdown valves and new hydraulic pressure units in Plant 2.

Together, those upgrades will cost approximately $12 million, of which roughly $10 million is dedicated to Plant 2 upgrades, Suncor said on Monday.



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